gutted Cat & replaced FPR

Started by GPChief, May 30, 2006, 03:00:15 AM

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GPChief

This weekend I was able to work on my car, I gutted the Cat, it was 3/4 clogged.  I also replaced the FPR & EGR.  What a difference no idle issues going up and down - just smooth :icon_biggrin:

Just curious, after others have done this did boost go down? I am only seeing 4 LBS now. 

2004 GTP -  3.8 Blown - Only modding for MPG.
1997 GTP  - 3.8 Blown - Too many mods to list.
1996 GTP - 3.4 DOHC - Twin to my 1997.
1995 SE - soon to be a 3.8 turbo car.
1990 TSTE x 2 white cloth
1990 TSTE x 1 maroon leather
1990 TGP - 5 speed.

TGPilot

With the increased exhaust flow you are probably taxing the W/G actuator to a point it is opening from backpressure. ONLY AS A TEST...wire the Wastegate closed with some Military Spec safety wire ;) and see if your boost increases.

If it does increase then check how are you running the pressure line to the W/G solenoid and actuator? 4 lbs is what the wastegate actuator preload is. I have never checked...but maybe the solenoid is normally open and you did not plug it back in allowing for free flow through the solenoid back to the actuator?

GPChief

This A.M. driving to work I hit full boost.  Ran the rest of the storage fuel out of it yesterday and found a shell station that sold 92 octane and filled it up.  I fugure it was the old gas & sitting for a year and a half.
2004 GTP -  3.8 Blown - Only modding for MPG.
1997 GTP  - 3.8 Blown - Too many mods to list.
1996 GTP - 3.4 DOHC - Twin to my 1997.
1995 SE - soon to be a 3.8 turbo car.
1990 TSTE x 2 white cloth
1990 TSTE x 1 maroon leather
1990 TGP - 5 speed.

TGPilot

Maybe she was still sleepy when you first drove it...now she is awake and ready to go! ;)